HELLO,
OURS IS GAS SWEETENING PLANT DESIGNED FOR REMOVAL OF H2S BY USING MDEA AS SOLVENT. IT IS DESIGNED FOR 1375 PPM OF H2S BUT AT PRESENT FEED IS HAVING 150 TO 180 PPM. DUE TO THIS WE HAVE REDUCED SOLVENT RATE TO 175 M3/HR FROM DESIGNED 228 M3/HR AT 50% BY WEIGHT SOLVENT CONCENTRATION.
AT PRESENT WE ARE FACING THE PROBLEM MORE HC ABSOBRTION IN MDEA, THAT IS GENERATING MORE THAN DESIGNED FLASH GAS IN THE INTERMEDIATE MP FLASH SYSTEM PROVIDED BEFORE LP REGENERATION SYSTEM. THIS IS EFFECTING FEED RATE AND QUALITY OF PRODUCT. PLEASE HELP ME BY ANSWERING FOLLWONG QUERIES:
1.) FACTORS EFFECTING HC ABSORBTION IN MDEA.
2.) HOW TO CONTROL IT.
RAMA